You need to enable JavaScript to run this app.

Skip to main content

RE: Bus Restoration
Some good news regarding our Transbus MPD, 574 / NK53 TMZ......

When we purchased 574, we were advised that either the engine had seized, or a piston had gone - Luckily for us, it's neither, and the alternator has seized, which is probably the best news we could have hoped for.

Following a thumbs up from two engineers, we took 574 on a road test, and she performed very well!

You can view a short video here..... Transbus 574 - Road Test

Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
Bus Restoration.
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration
RE: Bus Restoration